ok I think I got it right in my options. I replaced the eops with cylair , Longterm 1 wiht dynair and also longterm 2 with manvac.
How do I go about manually validateing serial pids ? Just select pids and plug into car to validate?
2000 NBM trans am.
427 Dart ship block,Lme ported Ls7 heads 12.5 compression
246/262 .730/.712 112+4 low lash solid roller
Rmvb 4l80 with transbrake, 8" FTI converter
12 bolt Moser rear end with 4.10 gears
Connect to car,
select pids,
save pid selection to file (for future reference),
File->Connect,
Info->Validate PIDs.
I will do that tomorrow Joe, Thanks. You guy's have been lots of help, I have learned a lot the last few days.
I will post results of how the nova runs tomorrow night if i can get the tune done in a few passes. Hope to be close enough to run the bracket race tomorrow night.
2000 NBM trans am.
427 Dart ship block,Lme ported Ls7 heads 12.5 compression
246/262 .730/.712 112+4 low lash solid roller
Rmvb 4l80 with transbrake, 8" FTI converter
12 bolt Moser rear end with 4.10 gears
Races were cancelled after I made the 90 mile trip. The freeze busted the tracks water mains. I will try again later.
2000 NBM trans am.
427 Dart ship block,Lme ported Ls7 heads 12.5 compression
246/262 .730/.712 112+4 low lash solid roller
Rmvb 4l80 with transbrake, 8" FTI converter
12 bolt Moser rear end with 4.10 gears
Went to the track yesterday. car was pulling timing again but I figured that out. Tq management in the transmission even though I dont have a 4l60 in it, (th350) was pulling timing. I also dont have a vss so the car did not know it was moving . I turned everything that I could find off that could pull timing and that fixxed it. with tq mng. I ran 12.06 @ 110 mph.
After fixxing the timing issue It went 11.24 @ 119.5mph with a 1.62 60 ft. Not spinning, the car is leaving like it has a 2 step. Intake air temp was at 115+ leaving the line and it was weak off the line. once I go wot it leaves soft and Then breaths a good gulp of air in and its like nitrous hits it. air fuel on that pass was around 12.0/1
next pass was a 11.12 @ 119.8 with a 1.59 60 ft leaned it out to 12.3/1
After that pass I pulled it back to about 12.6 but have not read the data logg on these yet. It reacted to nice with a 11.05 @ 120.2 and a 1.54 60 ft. (still have that 2step going on) and I was so wanting that 10 anything that I went back around without changeing anything. Car had a long break to cool off since a friend of mine smashed his oil pan ,the track crew spent an hour cleaning up.
After the cool down(not sure yet on iat yet) my car left with a 1.57 60 ft(still hesitateing) and ran 10.96 @ 120.69 mph.
I am moving my Iat sensor and my filter all the way out by the grill to get the hot header air away from going into the engine. That should fix that 2 step feeling and ram some air in at the same time.
2000 NBM trans am.
427 Dart ship block,Lme ported Ls7 heads 12.5 compression
246/262 .730/.712 112+4 low lash solid roller
Rmvb 4l80 with transbrake, 8" FTI converter
12 bolt Moser rear end with 4.10 gears
Good work mate. Great to see it is all coming together.
The Tremor at AIR
Joe they are on my laptop and I need a new charger for it. I broke the wires to my charger last night.
I have to reroute my cold air intake to the grill. Its breathing some hot air in but i do believe there is something else going on with it. That bog off the line is on every pass and then it comes alive.
Here is a video a friend took though of the 11.05 pass
http://s273.photobucket.com/albums/j...2009020525.flv
2000 NBM trans am.
427 Dart ship block,Lme ported Ls7 heads 12.5 compression
246/262 .730/.712 112+4 low lash solid roller
Rmvb 4l80 with transbrake, 8" FTI converter
12 bolt Moser rear end with 4.10 gears